Hi Guys,
im facing some issues with my omphobby m4.
Dont go hard on me, im new to "bigger helis". I've only flown M1 and M2 before.
on faster collective inputs like a flip or tik-tok my heli tail starts wandering out. Also the whole heli kind of knicks itself inward and is generally wobbling around. Hard to describe, i hope you can see it in the video.
I tried playing around with pitch precomp and tail gain settings - no success
PID on Ail, Ele and Rud did not change much from Jonas settings.
When changing from ~2.1k RPM to 2.6k RPM, it gets much more stable.
I put much efford into the build and double checked everything. (it was my first build tho)
Remote: Radiomaster TX15s with ELRS
FBL: MSH Brain 2
PID Settings i use those from Jonas Wackershauser slightly tuned to the current 2.2k rpm
Maybe a heli god has an instant answer to this. Thanks!